| I just finished up this job by using the 140 regulatory, which I purchased from Autohaus AZ, and I am totally happy now. The fan works great and I saved myself ~$450. The writeup on splicing the wires was very informative and easy to follow.
So the dead motor was indeed the blower regulator and not the fan in this case.
I ended up changing the charcoal and the regular filters, which added 15 or so minutes to the job.
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1998 E300DT
1987 Mustang GT Convertible (Enjoy all of 225 stock HP  )
1996 Honda ST1100
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